[1] Mikolajezak A A,Arnoldi R A,Snyder L E,et al.Ad.vances in Fan and Compressor Blade Flutter Analysisand Predictions[J].Journal of Aircraft,1975,12(4): 325-332.
[2] Lane F.System Mode Shapes in the Flutter of Compres.sor Blade Rows[J].Journal of the Aeronautical Scienc.es,1956,23:54-66.
[3] Carta F O.Coupled Blade-Disk-Shroud Flutter Instabil.ities in Turbojet Engine Rotors[J].ASME Journal of Engineering for Power,1967,89(3):419-426.
[4] Bendiksen O O.Aeroelastic Problems in Turboma.chines[R].AIAA 90-1157.
[5] Cinnella P,De Palma P,Pascazio G,et al.A Numeri.cal Method for Turbomachinery Aeroelasticity[J].Jour.nal of Turbomachinery-Transactions of ASME,2004, 126(2): 310-316.
[6] Srivastava R,Bakhle M A,Keith T G,et al.Aeroelas.tic Analysis of Turbomachinery PartII-Stability Compu.tations[J].International Journal of Numerical Methods for Heat & Fluid Flow,2004,14(3): 382-402.
[7] 张伟伟,苏丹,张陈安,等 .一种基于 CFD的叶轮机非定常气动力组合建模方法[ J].推进技术, 2012, 33(1):37-42.(ZHANG Wei-wei,Sun Dan,ZHANG Chen-an,et al.A CFD-Based Compositional Methodol.ogy of Unsteady Aerodynamic Modeling for Turboma.chinery[J].Journal of Propulsion Technology,2012, 33(1):37-42.)
[8] Strazisar AJ,Wood JR,Hathaway MD,et al.Laser An.emometer Measurements in a Transonic Axis-Flow Fan Rotor[R].NASA STI/Recon Technical Report 2879, 1989.
[9] Whitehead D S.Effect of Mistuning on the Vibration ofTurbomachine Blades Induced by Wakes[J].Journal of Mechanical Engineering Science,1966,8(1):15-21.
[10] Ewins D.The Effect of Detuning upon the Forced Vibra.tions of Blade Disks[J].Journal of Sound and Vibra.tion,1969,9(1):65-79.
[11] Kaza K R V,Kielb R E.Flutter and Response of a Mis.tuned Cascade in Incompressible Flow[J].AIAA Jour.nal,1982,20(8): 1120-1127.
[12] Crawley E F,Hall K C.Optimization and Mechanisms of Mistuning in Cascades[J].ASME Journal of Engi.neering for Gas Turbine and Power,1985,107(2): 418-426.
[13] Nowinski M,Panovsky J.Flutter Mechanisms in Low Pressure Turbine Blades[J],Journal of Engineering for Gas Turbines and Power,2000,122(1):82-88.
[14] Sadeghi M,Liu F.Computation of Mistuning Effects onCascade Flutter[J].AIAA Journal,2001,39(1):22-28.
[15] Tomokazu M.Flutter and Forced Response of Turboma.chinery with Frequency Mistuning and Aerodynamic Asymmetry[D].Durham: Duke University,2008.
[16] Castanier M P.Pierre C.Modeling and Analysis of Mis.tuned Bladed Disk Vibration: Status and Emerging Direc.tions[J].Journal of Propulsion and Power,2006,22(2):384-389.
[17] Kazawa J,Watanable T.Numerical Analysis toward Ac.tive Control of Cascade Flutter with Smart Structure[R].AIAA 2002-4079.
[18] Sadeghi M,Liu F.Investigation of Mistuning Effects onCascade Flutter Using a Coupled Method[J].Journal of Propulsion and Power,2007,23(2):266-272.
[19] 胡超,李凤明,邹经湘,等 .失谐叶片 -轮盘结构振动模态局部化问题的研究[ J].中国电机工程学报, 2003,23(1): 189-194.
[20] 王建军,李其汉,朱梓根 .失谐叶片 -轮盘结构系统振动局部化问题的研究进展[ J].力学进展, 2000,30(4): 517-528.
[21] 郑赟,王静.错频对叶片的气动弹性稳定性影响[J].航空动力学报, 2013,28(5): 1029-1036.
[22] 冯毓诚,胡宗安,赵秀华,等 .轴流压气机流体诱发振动的实验研究[ J].北京航空学院学报, 1986,4: 103-111.
[23] 杨晓东,侯安平,李漫露,等 .相位延迟条件在叶轮机械颤振分析中的应用[ J].航空动力学报, 2014,29(8): 1846-1854.(编辑:朱立影)* 收稿日期:2014-04-08;修订日期:2014-05-28。基金项目:国家自然科学基金重点资助项目( 60934001)。作者简介:杨晓东( 1987—),男,博士生,研究领域为流体机械及工程。 E-mail:yang123931@163.com
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